Recommission, 4/20/2007
Recommissioning for spring was a pretty smooth process. The bulk of the engine work was done in the fall, so spring only brought a few more chores.
The process began with shrinkwrap removal, a couple weeks before spring launch. It was just a matter of cutting the wrap down the center line with a carpet knife, and then cutting tie-down strings to release it. Michele and I cut the huge pieces of wrap into somewhat more manageable-sized pieces, rolled it up, and used the tie-down strings to tie the rolls. Carrying it to the recycle pile at the marina completed the job. Once unwrapped, we reattached a few things like the bimini frame and antennas, checked all the seacocks, hoses, etc, so the boat was ready to drop in the water. Shipwright finally launched the boat in mid-April, and we attended to the rest of the work almost immediately.
I started by draining the pink antifreeze from the potable water tank, adding a quart of bleach, and refilling with water. I ran some of the bleach/water solution through each of the taps to fill the pump and the lines with the solution, and then left it sitting until the next day.
The engine required the most work. The first task was making sure the engine would start. It fired right up and seemed to run smoothly, bringing a heavy sigh of relief! With that anxiety passed, it was time to change the fuel and air filters. Changing the filters was relatively quick, if a little messy. But diesel engines don't like air in the fuel lines, so whenever fuel filters are changed, the air must be purged. Having never done that, I was concerned that it would be a struggle, and it certainly was. To get the air out, one is supposed to loosen a vent screw on the fuel filter, and then operate a little mechanical "lift pump" until the air bubbles subside and fuel starts escaping from the vent. Well, I pumped. And pumped. And pumped. And pumped some more. This went on forever. I finally tried starting the engine, and although it fired up, it quickly died. My guess is that there is something wrong with the lift pump, because I never did succeed in purging the air. Ultimately, I ended up pouring filtered diesel into the filter itself and then reinstalling it. After that, a few cranks of the engine had it running again.
A quick test run of the air conditioner showed it working fine. Nothing else to do there.
The next day, Michele and I got an early start, cleaning and prepping, rehanging curtains, flushing the potable water system, etc. A few hours of this had us more than ready to set out on our first cruise of the year.
Friday, April 20, 2007
Saturday, April 14, 2007
Keep The Water On The Outside, Part 4: Hatch Gasket
Hatch Gasket, 4/14/2007
Hatches tend to develop leaks over time as gaskets get hardened or worn out. Such was the case with the Bomar hatch over our v-berth. The leak wasn't severe, but it was enough where we had to keep a towel over the cushions when away from the boat.
There are a number of ways hatches can leak. Ours, at first, appeared to be letting water underneath the rubber gasket on the hatch that presses against the hatch frame when it is closed. The old gasket, roughly 1/2" square, was hardened to where it didn't really compress at all.
The most difficult part of this repair was locating the right gasket, and the first step was identifying the brand and model of the hatch. Our owners manual identified it as a Bomar hatch, but did not provide a model number. Pompanette, the maker of Bomar hatches, was tremendously helpful in figuring out the model. Two phone calls plus an email with the attached pictures lead the representative there to conclude that this is a Bomar Hi-Profile hatch, requiring a "lip-gasket", part number p2000-26. I ordered 8 feet from a marine supply, and it was exactly the right stuff.
The old gasket pulled out easily, but left some glue-like residue behind that cleaned up pretty easily with a little WD-40 and Simple Green. I installed the new gasket following the included instructions, and it went in easily for the most part. The corners were tricky, but a small screwdriver helped in tucking the lip of the gasket into the notch between the frame and the glass. I found that it's important not to stretch the new gasket while installing it, or it will shrink back, pulling itself out of the groove when it does. The new gasket provided a much tighter seal.
Unfortunately, it seems that the extra pressure from the new gasket produced another leak, through the handles (called "hatch dogs") where they go through the glass. The handles are seated in o-rings, which are supposed to seal against water while still allowing them to turn. That is a straightforward fix: Unscrew and take apart the handles, replace o-ring, reinstall.
Now we have a dry bed!
Hatches tend to develop leaks over time as gaskets get hardened or worn out. Such was the case with the Bomar hatch over our v-berth. The leak wasn't severe, but it was enough where we had to keep a towel over the cushions when away from the boat.
There are a number of ways hatches can leak. Ours, at first, appeared to be letting water underneath the rubber gasket on the hatch that presses against the hatch frame when it is closed. The old gasket, roughly 1/2" square, was hardened to where it didn't really compress at all.
The most difficult part of this repair was locating the right gasket, and the first step was identifying the brand and model of the hatch. Our owners manual identified it as a Bomar hatch, but did not provide a model number. Pompanette, the maker of Bomar hatches, was tremendously helpful in figuring out the model. Two phone calls plus an email with the attached pictures lead the representative there to conclude that this is a Bomar Hi-Profile hatch, requiring a "lip-gasket", part number p2000-26. I ordered 8 feet from a marine supply, and it was exactly the right stuff.
The old gasket pulled out easily, but left some glue-like residue behind that cleaned up pretty easily with a little WD-40 and Simple Green. I installed the new gasket following the included instructions, and it went in easily for the most part. The corners were tricky, but a small screwdriver helped in tucking the lip of the gasket into the notch between the frame and the glass. I found that it's important not to stretch the new gasket while installing it, or it will shrink back, pulling itself out of the groove when it does. The new gasket provided a much tighter seal.
Unfortunately, it seems that the extra pressure from the new gasket produced another leak, through the handles (called "hatch dogs") where they go through the glass. The handles are seated in o-rings, which are supposed to seal against water while still allowing them to turn. That is a straightforward fix: Unscrew and take apart the handles, replace o-ring, reinstall.
Now we have a dry bed!
Sunday, April 8, 2007
Prop Nut Zinc
Replaced Zinc, 4/8
Cape Dory 28' cruisers require only one sacrificial zinc anode to protect the underwater metals from corrosion. It's a "perry nut" type, on the end of the prop shaft. Last year's zinc was about 1/2 gone, so it needed to be replaced for the start of the season.
Our boat's shaft is 1 1/2" diameter, which takes a prop nut zinc size "F". I found it in a few places online, including Hamilton Marine and BoatZincs.com. The zinc is relatively inexpensive, at around $15. Generally, only the zinc needs replacing, not the entire bronze prop nut, which is much more costly at about $90.
Cape Dory 28' cruisers require only one sacrificial zinc anode to protect the underwater metals from corrosion. It's a "perry nut" type, on the end of the prop shaft. Last year's zinc was about 1/2 gone, so it needed to be replaced for the start of the season.
Our boat's shaft is 1 1/2" diameter, which takes a prop nut zinc size "F". I found it in a few places online, including Hamilton Marine and BoatZincs.com. The zinc is relatively inexpensive, at around $15. Generally, only the zinc needs replacing, not the entire bronze prop nut, which is much more costly at about $90.
See The Light (Part 2)
Stern light, 4/8/2007
In the fall, I installed a new combination masthead / all-round light, so that I could illuminate only the forward-facing portion (the masthead) while piloting at night. This setup requires a separate stern light, which I finally installed just before spring launch.
I ran the wiring for the stern light back in December while working on the cockpit courtesy lights, so most of this project was already done. I picked up an Aqua-signal Series 20 stern light (which matches the currently installed sidelights), and installed it on the transom. The transom is solid fiberglass, not cored, so simple screws weren't going to work very well. I had to drill through the transom to run the wires anyway, so I thru-bolted the light with 2.5" #6 stainless machine screws. On the inside, the nuts are under the gunwale anyway, so they don't affect the interior appearance. For a change, I managed to drill the holes without any serious fiberglass chipping. I put painter's tape over both sides (inside and outside), and drilled through from the outside. I scored the holes with the drill in reverse first, and then ran it forward to finish the holes. The inside chipped slightly when the drill went through, but nothing serious.
To finish the navigation lights project, I inspected the sidelights which needed a little maintenance. Both lenses needed cleaning, and the teak fairing block on the port side was cracked, so I repaired it with epoxy. I also picked up a spare bulb and added it to my emergency kit.
Now I can hardly wait for an opportunity to be out on the bay after dark. It's a completely different experience, and one that I loved in Seattle, so I'm looking forward to the bay at night!
In the fall, I installed a new combination masthead / all-round light, so that I could illuminate only the forward-facing portion (the masthead) while piloting at night. This setup requires a separate stern light, which I finally installed just before spring launch.
I ran the wiring for the stern light back in December while working on the cockpit courtesy lights, so most of this project was already done. I picked up an Aqua-signal Series 20 stern light (which matches the currently installed sidelights), and installed it on the transom. The transom is solid fiberglass, not cored, so simple screws weren't going to work very well. I had to drill through the transom to run the wires anyway, so I thru-bolted the light with 2.5" #6 stainless machine screws. On the inside, the nuts are under the gunwale anyway, so they don't affect the interior appearance. For a change, I managed to drill the holes without any serious fiberglass chipping. I put painter's tape over both sides (inside and outside), and drilled through from the outside. I scored the holes with the drill in reverse first, and then ran it forward to finish the holes. The inside chipped slightly when the drill went through, but nothing serious.
To finish the navigation lights project, I inspected the sidelights which needed a little maintenance. Both lenses needed cleaning, and the teak fairing block on the port side was cracked, so I repaired it with epoxy. I also picked up a spare bulb and added it to my emergency kit.
Now I can hardly wait for an opportunity to be out on the bay after dark. It's a completely different experience, and one that I loved in Seattle, so I'm looking forward to the bay at night!
Bronze Is Beautiful
Propellor, 4/8/2007
Throughout our first summer ('06), we were never able to get the engine RPM up into the recommended range. Usually, that's a sign that you're "overpropped". Before launching this year, I had Digital Prop Shop recondition the prop and reduce the pitch from 18 to 16, which should let the engine spin up to the rated RPM. Also replaced the "prop nut zinc", a large sacrificial zinc on the prop nut, which helps prevent corrosion of other under water metals.
Throughout our first summer ('06), we were never able to get the engine RPM up into the recommended range. Usually, that's a sign that you're "overpropped". Before launching this year, I had Digital Prop Shop recondition the prop and reduce the pitch from 18 to 16, which should let the engine spin up to the rated RPM. Also replaced the "prop nut zinc", a large sacrificial zinc on the prop nut, which helps prevent corrosion of other under water metals.
Cover Me
Canvas Repair, 1/6/2007
The Sailrite catalog arrived yesterday. I don't plan to do a lot of sail-making, but as I flipped through the catalog looking at all the interesting things in it, it occurred to me that what I like so much about doing our own maintenance is the freedom and independence it provides. We do whatever we want, with no worries about finding competent, affordable help.
Our aft canvas was in rough shape. First of all, it was filthy. But more importantly, it was leaking and the fasteners were no longer doing their job. The velcro was falling apart, and the "lift-the-dot" snaps were tearing through the canvas (these snaps take a tremendous amount of strain holding almost the entire weight of the canvas in the air). My plan had been to take the whole thing to a canvas repair shop and have them restore it, but as I considered it more, it seemed like a managable "DIY" project, especially now that Michele has her handed-down sewing machine.
I scrubbed the whole thing in the backyard and it cleaned up nicely. I found velcro and marine grade vinyl at Jo-Ann fabrics, and new lift-the-dot snaps at Sailrite. Michele had a little sewing tool that worked great for cutting the thread to remove the old velcro, and I just used a screwdriver and pliers to remove the old snaps. Michele did all the sewing work to attach the new velcro and little vinyl reinforcements for the snaps, and I put the new snaps on. We sprayed the whole thing with 303 Fabric Guard, and ta-da, the canvas is like new!
Emboldened by our success, we bought new canvas material and snaps so we can try to make a canvas cover for the windshield from scratch. Looking forward to that!
The Sailrite catalog arrived yesterday. I don't plan to do a lot of sail-making, but as I flipped through the catalog looking at all the interesting things in it, it occurred to me that what I like so much about doing our own maintenance is the freedom and independence it provides. We do whatever we want, with no worries about finding competent, affordable help.
Our aft canvas was in rough shape. First of all, it was filthy. But more importantly, it was leaking and the fasteners were no longer doing their job. The velcro was falling apart, and the "lift-the-dot" snaps were tearing through the canvas (these snaps take a tremendous amount of strain holding almost the entire weight of the canvas in the air). My plan had been to take the whole thing to a canvas repair shop and have them restore it, but as I considered it more, it seemed like a managable "DIY" project, especially now that Michele has her handed-down sewing machine.
I scrubbed the whole thing in the backyard and it cleaned up nicely. I found velcro and marine grade vinyl at Jo-Ann fabrics, and new lift-the-dot snaps at Sailrite. Michele had a little sewing tool that worked great for cutting the thread to remove the old velcro, and I just used a screwdriver and pliers to remove the old snaps. Michele did all the sewing work to attach the new velcro and little vinyl reinforcements for the snaps, and I put the new snaps on. We sprayed the whole thing with 303 Fabric Guard, and ta-da, the canvas is like new!
Emboldened by our success, we bought new canvas material and snaps so we can try to make a canvas cover for the windshield from scratch. Looking forward to that!
Saturday, April 7, 2007
Launch?
April 7 and the forecast is... snow?! The boat was supposed to be launched this week, and I was planning to recommission the engine and other systems this weekend. Not sure if the yard actually got to it or not -- might still be on the hard. The freshwater system already has water in it. Hopefully the temps won't be cold enough to do any damage. I guess I'll be waiting until next weekend!
Friday, April 6, 2007
What's Done Is Done
Here's the list of work I've done on the boat during the first year. If I think of anything I forgot, I'll update it later. Eventually, I'll probably make a separate post for most of the items, describing the work that each involved. Some of this is repair/restoration work. Some is basic maintenance. Some doesn't even qualify as maintenance, just routine tasks (like pumping out the holding tank) that I included because I needed to figure out how to do it. Michele helped with a lot of this list -- she's not afraid to get her hands dirty, that's for sure!
These are things I still plan to do. By no means a comprehensive list...
- Had gelcoat damage along bootstripe repaired and bootstripe repainted
- Had bottom painted with antifouling paint
- Repaired frozen seacocks
- Had deteriorated fuel hoses replaced
- Had propellor repitched from 18 to 16
- Replaced toilet
- Replaced galley and head faucets
- Replaced instrument bezel rings
- Replaced engine room hatch gasket
- Replaced door catches in v-berth storage
- Repaired loose fiberglass along bulkhead in head compartment
- Replaced hatch gasket
- Found and fixed freshwater system leak
- Repaired head compartment door latch
- Mounted fire extinguisher
- Replaced center windshield gasket
- Cleaned and repaired aft canvas and applied waterproofing
- Cleaned interior
- Cleaned exterior, including mold and mildew on flybridge
- Cleaned engine room, bilge, and keel
- Cleaned A/C filter
- Cleaned and scrubbed mildew from all curtains and fabric
- Removed cockpit coaming
- Bought new lines and fenders
- Replaced anchor rode and shackles
- Replaced missing screws in cockpit portside step and teak trim
- Replaced gaskets on cockpit hatches
- Tethered aft cockpit hatch
- Pumped out holding tank
- Removed name decal from transom
- Washed, polished, and waxed hull sides
- Touched up bottom-paint
- Checked all fuses and bought spares
- Duplicated ignition key
- Found key blanks for wheelhouse door key
- Duplicated wheelhouse door key
- Replaced prop nut zinc
- Changed oil and filter
- Changed crankcase breather
- Cleaned seawater strainer
- Changed transmission fluid
- Changed coolant/antifreeze
- Replaced air filter
- Replaced fuel filters and purged air from lines
- Winterized air conditioner
- Winterized fresh water system
- Winterized head/holding tank
- Checked battery water levels
- Drained seawater, circulated antifreeze through raw water system
- Replaced engine zincs
- Replaced coolant/antifreeze cap
- Replaced engine seawater intake hose and fixed chafe protection
- Serviced seacocks
- Repacked rudder stuffing box
- Repack shaft stuffing box
- Greased shift and throttle cables
- Greased steering cable
- Replaced A/C intake hose and plastic elbow fitting
- Cleaned engine, sanded and repainted rusted areas
- Cleaned corrosion from all brackets, bonding wires, engine mounts, etc, and sprayed with corrosion block
- Primed and painted rudder mounting brackets.
- Cleaned and assembled emergency tiller
- Re-bedded leaking stanchion bases
- Replaced batteries, battery cables, and battery switch
- Replaced all-round light with new combination masthead/all-round light
- Rewired Nav/Off/Anchor light switch for new light configuration
- Installed new stern light
- Repaired side navigation lights (upcoming shortly)
- Replaced flybridge compass
- Removed Loran and old VHF radio
- Removed Loran antenna and extra VHF antenna
- Installed new VHF with flybridge remote microphone
- Installed GPS (upcoming shortly)
- Installed blower
- Replaced stereo and corrected speaker wire runs
- Replaced galley and head outlets with GFCI outlets
- Replaced shorepower cable
- Replaced deteriorated electrical wire
- Replaced household wire nut connectors with heat-shrink butt connectors in bilge
- Rewired bilge pump directly to battery
- Added chafe protection for wire runs to cockpit
- Straightened and supported all electrical wire in engine room
These are things I still plan to do. By no means a comprehensive list...
- Reseal/regasket wheelhouse windows
- Replace main VHF antenna
- Replace hot water heater
- Replace port wiper motor
- Re-crimp battery cables
- Connect flybridge horn switch
- Caulk around galley and head sinks
- Maintain exterior teak
- Replace battery boxes
- Chafe protect lines
- Replace anchor locker latch
- Wash and wax top sides
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